

You need about 5" h2o vac min for a reasonable gasifier start up and run in fan. 10" is better and will let you do the whole basic range of run concern. 20" will let you do the full range for complete testing and characterization.
The ejector/venturi that comes with the GEK will do 20", but requires compressed air. This is fine for testing environments and first world run situations. It is less good for dev world and general boonies run situations. A fan is much easier and with less equipment dependencies. However, for it to work reasonably in off grid situations, it needs to be 12vdc. 120/240vAC fans don't help if you don't have ready power before you start your gasifier. Most high vac high heat tolerance fans are 120/240vAC solutions.
Thus we're trying to get to the minimum build and cost requiremets for a basic starting fan for a gasifier. We think this should have about 10" of usable vac. The original gek fan would do about 4" vac, which proved to be not enough once filter, nozzle and burner losses were added.
Standard squirrel cage fans produce about 1". Shop vacs will do 20"+, but they get fouled, are made of plastic, and generally fall apart. Proper forge combustion fans start in the $500 range, which is too expensive. We need something we can sell in the 100-200 range. For a 12vdc solution, this requires working with car/truck Fasco type fan motors, and designing the fan in relation to the available power, not the other way around. For the full range of proper high pressure/vac large fans, see cinncinnati fan here: http://www.cincinnat...03-internet.pdf
So here's what we've done so far within these constraints:
-created a fan that for the most part bolts together during production. This allows for less labor on the welding side but also for a thinner fan.
-introduced the use metallic gasketing via foil tapes to create a high temp seal.
-increased the rotor size to ten 10"DIA plus. will likely increase it some more.
-lowered the overall width of the fan cowling to 1-3/8" and the blades to 0.7" for less bite and power consumption.
-introduced a bolt on no weld hub. for improved balance and service life.
-introduced a needle bearing and a solid motor support for other performance improvements and adjust-ability for alignment.
And the results: My word what were we waiting for?
Under a static load. that is with no air being allowed to enter the intake and just measuring the vacuume.
We achieved a 8.75"/h20 at 4100rpm. That's about 'double' the amount of static pressure from our last fan.
And have deemed this successful enough that we can ASAP (after our upcoming workshop) do one more round to finalize the design, and then offer this fan as a low cost, real solution for gasifier start up and moderate running fan.
For more pictures and general details about the fan, see here:
http://gekgasifier.p...Fan-Prototyoing
cheers!












